November 30, 2010 Special Supplement
November 29, 2010
As you can see in the photos, I still need to insert bungs to cover the screw holes on one side. That presents a bit of a challenge because normally the bungs are trimmed and finished with the rest of the piece. I can't do that in this case without having to refinish the whole thing, which of course I don't want to do. I plan to pre-finish a thin strip of jatoba from which I will cut the bungs. Hopefully I'll be able to insert and glue the thin, pre-finished bungs so they are flush with the surface. We'll see....
I also tried out my new screw extractors on the broken-off old bronze screws that secure the teak hatch hinges. They worked great. Very cleverly, the saw teeth are designed to cut counter-clockwise, so it encourages the screw remnants to come right out as you make the surrounding circular cut.I glued dowel pieces (which didn't need to match since they will be covered by the hinge) into the resulting holes and then trimmed them flush with a chisel. You can see in the photo that it's not as clean as what the flush-cut saw would have done, but I couldn't use the flush-cut saw because of the recess for mounting the hinge flush with the wood surface. Again, it won't be visible, so as long as it's a strong joint, it doesn't need to be elegant.The old generator is still sitting in cockpit waiting for a break in the weather so it can be removed. The prospects for the coming weekend don't look good at the moment, with yet another storm moving in later in the week. Looks like I won't be able to tackle the next port installation for a while either. Ah well, there's always something that can be done!
November 21, 2010
Happy Thanksgiving all!
November 15, 2010
The main mission for the weekend was to remove the big old Westerbeke 4.4 kw genset which had never been completely installed and whose operability was dubious. I don't need or want a big monster like that, and I had previously struck a deal with Bill, the itinerant master diesel mechanic, that he could have it if he removed it. Once out, I can use the space for something better like a work bench with organized tool storage and a vise.
Friday was the big day, so I took the day off to lend a hand and keep an eye on things. I was there early, and so spent a couple of hours working on the forward hatch that still had a bit of a leak despite rebedding with butyl and a new gasket. I relied on the wisdom of Sherlock Holmes to solve the mystery: "When you have eliminated the impossible, what remains, no matter how unlikely, must be so." In this case, although unlikely, the leak had to be around the butyl between the metal hatch frame and the teak mounting base. Because of the way the base is constructed and where the water was entering, it was impossible to be leaking elsewhere. I concluded I needed to compress the seal more using the clamping method that had recently proven effective on the portlight installation. I removed the hatch's mounting screws and clamped and squeezed and clamped and squeezed until I had gone entirely around the perimeter. I replaced the screws tightly and set the hose running water over the hatch to test the seal. About this time Bill arrived, along with Scott, one of the two brothers who own and manage the marina. The two of them spent the better part of the day on the big hoist.
November 8, 2010
Sunday it rained steadily, but I wanted to go to the boat to check for leaks, replace the steering wheel and finish wiring up the radar.
The one teak hatch that wasn't covered with plastic sheeting seemed fine. I did discover that one of the covered-over holes for the old ports was leaking, so I now know which new port gets installed next. Much to my surprise and disappointment, I discovered the forward hatch that I had redone was leaking somewhere between the frame and the base. I tried tightening the mounting screws in the rain, to no avail. There was one screw the wrong size that could not be tightened securely, so that might be it. There's a lot of butyl around the base, but I didn't pre-compress it with clamps like I did with the new ports (which, by the way, did not leak). When I get some dry weather, I'll remove all the mounting screws, stuff in more butyl, and use clamps to compress the butyl.
I had to replace the steering wheel that I had just removed (with some difficulty, you might recall) because the mechanic who is going to remove my old generator wants to do it next week. To pull it off the boat, we need to move the boat to another part of the marina. Steering will be a necessity! The steering wheel's mounting screw would not go back into the shaft because it took so much force on the wheel puller to get the wheel off that the pressure from central pin on the puller distorted the first few threads in the steering wheel shaft just enough to prevent the mounting bolt from screwing in. No worries, I thought; I'll just re-tap the threads. No big deal, since I had a tap and die set on board. English boat, English threads, right? It turns out, no. So, I had to drive into town and get a metric tap the right size. Fortunately, they had one, and it did the job.
Next: wire up the radar display. Months ago while hauled out in Napa, I mounted the antenna on the mast while the mast was down, and eventually got the antenna wire through the mast. (See January 31 and February 15 blogs.) But under the gun to get the boat in the water and to her home berth, I never had time to wire up the display and check to see if everything worked. So, for all these months, it's been a little concern nagging at me. The day of reckoning had finally arrived. Luckily there was a breaker available on the panel and a route for the wire into the doghouse that didn't require any drilling. However, the instructions also called for a ground wire to be run from a terminal on the display "to a bolt on the hull (or weld)." Clearly they were assuming a metal hull, since fiberglass is an insulator. I found a bolt on the engine that had several other ground wires terminated to it, so I thought that would be a good spot to ground the display. I had just enough black wire to reach, too. Once I had everything wired up, it was time for the dramatic moment: would it work? I pressed the power switch. The display immediately lit up and showed the proper first screen. Yeah! Okay, but the big test was would the antenna and the cable connection work? I hacked around with the buttons and on-screen menu until I had arrived at the display that should show the radar image. Blank white screen. I went through the sequence again just to be sure I had done it right. I had. Still a blank screen. The roar of stomach acid flowing was palpable. I had visions of big problems and big expenses. I was able to push back the tide of anxiety and negative fantasies long enough to recall the wisdom of Occam's razor, which in this case meant "Look for the simplest problem/solution first." I jiggled the antenna connection on the back of the display. Voila!!! A radar image! Whew!!!
While I won't be able to permanently mount the display until I get a new ceiling in the doghouse, it was a great relief to know the radar is working.
Since I will need to move the boat next week, I thought it would be a good idea to make sure the engine and running gear were working properly before I left. Besides, the engine hadn't been run in quite a while, and it needed some exercise. I could let it run while I cleaned up. I checked the oil, which was still clear since the last change (only about 10 operating hours ago), and opened the raw water intake seacock. The engine started right up, water was gushing out the exhaust as it should, and she ran smoothly. There was only one fly in the ointment: the electronic digital engine hour meter was blank! Damn! Always something. I checked the connections on the back of the panel and everything seemed solid. Short of some sort of internal computer failure, the only thing I could think of that might have caused the failure was that there might be a ground connection at the engine bolt I used to ground the radar that had gone bad as a result of the removal and reassembly. Well, I was out of time and couldn't try to test that possibility. If a simple fix like cleaning and reconnecting the grounds doesn't do it, I'll have to just buy a good old reliable Hobbs meter and wire it into the ignition circuit. Stay tuned!
November 1, 2010
The epoxy around the hole on the sunny side cured quickly enough for me to try to bolt in the port. I soon discovered that my newly-purchased bronze machine screws were too short to extend through both the uncompressed butyl and the mounting flange. Damn! After a few moments of high anxiety, I thought I might be able to use a couple of clamps to compress the butyl enough to get the screws through. By repeatedly clamping and reclamping around the perimeter and using a lot of clamping pressure, it worked like a charm. The individual butyl pieces welded to each other nicely, and the excess squeezed out between the flange and the hole as I had hoped. Of course some also sqeezed out around the inside mounting flange on the cabin side, but that was easily removed simply by cutting around the flange with sharp knife and lifting off the excess. At this point, the epoxy around the hole on the shady side still wasn't cured, it was getting late, the rain was coming in, and I was beat-all good reasons to call it a day and head home.
It rained Friday and Saturday, so I continued with the shop projects. I rounded the corners on the mast support post cover, cut matching bungs from scrap jatoba and glued them in place on one side. On the other side (the piece that will be screwed on during installation) I mounted a teak grab handle. No, I didn't make it. At twelve bucks (even at Worst Marine), it wasn't worth the time. The next morning, after the glue had set, I trimmed the protruding bungs flat using a flushcut saw. I find it works better than using the usual chisel method. Even with a sharp chisel and thin cuts, I usually end up with some of the bungs breaking off below the surface. The flushcut saw doesn't scratch the surface and results in the bung trimmed so close to the surface that normal finish sanding is enough to make it perfect. Finally, finish sanding of the post cover pieces, and between-coats sanding of the varnish on the table parts. Last thing Saturday was to apply varnish all around.
Sunday was a beautiful day. I installed the second port as I had the first and applied a bead of 3M 4000 UV around the ports to finish off the installaton and create a redundent outer seal. With some white plastic caps to cover the protruding nuts and bolts, it will be a pretty clean installation. I cleaned up the week's mess (well, mostly), and called it a good week.