
Testing with the ohm meter showed zero resistance through the motor, confirming it was fried (or is it “toast”?) as a result of an internal short. Motors can be rewound, but unless everything else was perfect, it wouldn’t be worth it in this case. Further examination revealed that all four of the cast iron mounting flanges for the motor/gear/gypsy assembly had broken. The patient was definitely terminal.
I spent the rest of the day fabricating and assembling a new teak louver and rabbeted trim piece to repair and replace broken parts on the aft cabin hanging locker door.


No comments:
Post a Comment