Showing posts with label skipper head. Show all posts
Showing posts with label skipper head. Show all posts

The Saga of the Toilet of Circadian

In my last post I talked about tackling the leak from the pump handle shaft seal in my Skipper head.  While I got that leak fixed, it turned out that there were more.  It became a frustrating cycle.  Either the fixes didn't work or a new leak appeared once the previous ones were fixed.  I've had to pull the head out, flip it over, open it up and try new methods at least five times.  I THINK I've got it sealed now, and I've learned a couple of useful things along the way.  First, I found an easier way to prime the intake pump after opening up the head:  simply fill the bowl to within a couple of inches of the rim using the shower faucet.  (much easier than the hose connected from city water to the intake.)  Second, you can't reuse the factory paper gasket even if it looks fine because it has already been compressed.  Finally, everything needs to be tightened to the max!
Whenever I run into a frustrating problem like this, I always remember one of the pearls of wisdom I got from a friend years ago who was a former engineer in the Navy: "Sometimes you just have to be more stubborn than the problem is."
Although it appears to be leak-free now, I have been fooled before, so I'm a bit cautious about feeling flushed with success until more time has passed.  Check back in a week or two to see how the drama unfolds.  In the meantime, here are the details:

To find out why the joint at the base of the
head continued to leak even after I had
tightened the mounting screws, I had to
dismount it, flip it over and remove the
base plate.

While the gasket appeared undamaged...

...careful inspection revealed traces of the
leak where I had seen it before.

Evidence of the leak on the base plate as well as the head side.

So...I re-cleaned both mating surfaces again and tried
a different method.

This time I tried silicone form-a-gasket.

After putting it back together, remounting it and painting
it, it still leaked!  But in a different place!

Tore it down again and found the silicone a bit thin in the
area of the leak.

Cleaned it off again.

This time I was more generous with the silicone and put
a coat on both sides of the joint.

I put it back together without tightening
down the mounting screws fully for
 about an hour. While I waited for the silicone
to fully cure after tightening down the
screws, I moved the porta-pottie
from the aft head into the main head
so at least I had something to use in
the meantime.

When I tested it again, I found if it was 
STILL leaking at the base.  In addition,
there was now also a pin hole leak at the 
output hose connection.

Emergency rubber repair tape took care of the hose
connection leak, but I had to find another solution
for sealing the base joint.

By this time I was pretty quick at disassembling the thing
and cleaning the surfaces.

I decided to use rubber gasket material that was nearly
1/8 inch thick.  That allowed for plenty of compression
and there would be no thin areas or missed areas.
To mark the pattern for cutting, I covered the sheet
with masking tape, laid it on top of the base plate,
and pounded around the joint surface with a 5 lb hammer.
The resulting embossed pattern was good enough
to serve as a cutting guide.

While not factory perfect, the result was definitely good
enough: no gaps and the holes aligned.  I was optimistic.

Imagine my disappointment when I found it was leaking 
AGAIN right where it did the first time.  Okay,
time to try tightening the base mounting screws more,
even though I had made sure they were tight before.
This time I disconnected the hoses, flipped
 the head over and tightened the screw in question a bit
 beyond what I thought was prudent.  I went to the max
 even though I was concerned about stripping the slot or
breaking the screw.  It seemed to have stopped the leak
at the base.  HOWEVER...

Now there was a new leak at the intake elbow.  It was difficult
to get a wrench on the nut without disassembling the
head, but I managed to turn it just enough to stop the leak.

But wait...there's MORE!  Also a new leak at the output
elbow.  The engineering geniuses that designed this
put the connection bolt so close to the body that you
can't get a wrench or socket around it.  Fortunately I had a
 set of claw wrenches that could be mounted on the end
of a socket wrench extension, so I was able to barely
get to it and torque it down just enough to work.

I found I had just enough extra output hose length to cut 
off the first inch, hoping it would cure the leak I had 
previously patched with emergency tape.  Good idea;
it just didn't work.  So it was back to the emergency
tape trick, which did work once again.

After pumping through quite a bit of
water and allowing it to sit over night
with no signs of a leak, I remounted
the head and touched up the paint.

So far, so good.  Not counting chickens yet,
though.


Wildlife and Head Problems

I finally found a place where there are birds and iguanas that is within easy rowing distance, so I was able to get a few more wildlife photos.  On the down side, my head failed rather dramatically. (No, the marine toilet!)  It took three days of sometimes yucky, frustrating or back-breaking work, but it is now fixed and working properly.  Here's the story:

I devoted one entire morning to more exploration of the
canals around Marina Mazatlán.

Much of what was once estuary has become golf courses
and very expensive homes and condos.

Fortunately some wildlife remains.  This is a turkey
vulture warming up on the rocky rip-rap of the canal.

Turkey vulture eating a dead fish.  Not a pretty sight, but
better than a stinking, rotting dead fish!
 


A rare sight:  an iguana in the water

Showing off his mohawk?

A yellow-crowned heron peaks out from its hidey hole.

Gotta be stealthy to catch them exposed.

Tri-colored herons are even more skittish.  I got this image
just before this one took off.

Mexican grackles, on the other hand, can be
obnoxiously unafraid of people.  This one landed
right on my table while I was eating lunch.
I guess it knew a sloppy eater when it saw one.


Just another average sunset in the marina


My faithful Skipper head suddenly failed
in mid flush.  The big pump lever felt
like something gave way and it was no
longer connected to the pump piston.

First steps were dismounting the whole thing and then
pulling the handle to make it a little easier to get the
58-pound monster through the narrow companionway
and on deck.

Of course hose connections had to be broken, a 
rather delicate operation considering what both the
toilet and hoses contained.  Rubber gloves, 
disposable rags and a containment vessel
successfully averted a potential catastrophe.
Still yucky, though.

Head removed.  A Ziploc bag catches drips
from the hoses.

Getting the heavy thing up on deck without damaging
something took some planning and care as well as muscle,
but I did it.

Toilet inverted, the bottom plate removed and the guts
exposed.

The culprit:  the crescent-shaped key that
locks the pump lever to the shaft that 
connects to the pump piston lever had
come out, so the pump lever just spun
on the shaft.

The key was able to come out because the keyway had been
widened by corrosion and possibly by being sheered away
when pumping while the shaft had slipped out of position.

Fortunately the rebuild kit contained a replacement
lever.  Part of the reason the kit is more than $130.

The new lever and a new raw water intake
 flap spring installed and gasket mating surfaces
prepped for reassembly.  Only problem was
the spring retaining screw would not go back
in all the way, which prevented proper movement
of the lever.  I had to re-tap the hole threads
and replace the machine screw to fix it.

Back together and getting repainted.

Reinstalled and working fine...once I
remembered the trick to re-priming
the pump so it would take in sea water.
Just in time, too.  But that's another story!

July 9, 2015

Finally got all the watermaker issues resolved!  While it was frustrating in the short term, it will pay dividends in the long run.  Not only is the system more robust, but I now have a much better understanding of how it works and more confidence that I can troubleshoot and correct any future issues.  The tougher the battle, the sweeter the victory, ehh?
I’ve started doing the pre-cruise systems checks and of course now have more on the to-do list.  Having been essentially idle since last year, the Skipper head once again would not pump in raw water for flushing.  Having experienced this problem before, I was prepared to deal with it.  I had a short piece of hose that could be connected to city pressure water and then to the head intake.  That allowed priming the head under pressure.  A bit messy, but it works.  I had less success with the funky old shower sump pump, so it will be replaced.  I also continued re-stowing items displaced by the watermaker installation, topped off the batteries and finally, after putting it off for four years, finished securing the heavy electrical cables for the windlass. 
A busy, but productive week!