The Saga of the Toilet of Circadian

In my last post I talked about tackling the leak from the pump handle shaft seal in my Skipper head.  While I got that leak fixed, it turned out that there were more.  It became a frustrating cycle.  Either the fixes didn't work or a new leak appeared once the previous ones were fixed.  I've had to pull the head out, flip it over, open it up and try new methods at least five times.  I THINK I've got it sealed now, and I've learned a couple of useful things along the way.  First, I found an easier way to prime the intake pump after opening up the head:  simply fill the bowl to within a couple of inches of the rim using the shower faucet.  (much easier than the hose connected from city water to the intake.)  Second, you can't reuse the factory paper gasket even if it looks fine because it has already been compressed.  Finally, everything needs to be tightened to the max!
Whenever I run into a frustrating problem like this, I always remember one of the pearls of wisdom I got from a friend years ago who was a former engineer in the Navy: "Sometimes you just have to be more stubborn than the problem is."
Although it appears to be leak-free now, I have been fooled before, so I'm a bit cautious about feeling flushed with success until more time has passed.  Check back in a week or two to see how the drama unfolds.  In the meantime, here are the details:

To find out why the joint at the base of the
head continued to leak even after I had
tightened the mounting screws, I had to
dismount it, flip it over and remove the
base plate.

While the gasket appeared undamaged...

...careful inspection revealed traces of the
leak where I had seen it before.

Evidence of the leak on the base plate as well as the head side.

So...I re-cleaned both mating surfaces again and tried
a different method.

This time I tried silicone form-a-gasket.

After putting it back together, remounting it and painting
it, it still leaked!  But in a different place!

Tore it down again and found the silicone a bit thin in the
area of the leak.

Cleaned it off again.

This time I was more generous with the silicone and put
a coat on both sides of the joint.

I put it back together without tightening
down the mounting screws fully for
 about an hour. While I waited for the silicone
to fully cure after tightening down the
screws, I moved the porta-pottie
from the aft head into the main head
so at least I had something to use in
the meantime.

When I tested it again, I found if it was 
STILL leaking at the base.  In addition,
there was now also a pin hole leak at the 
output hose connection.

Emergency rubber repair tape took care of the hose
connection leak, but I had to find another solution
for sealing the base joint.

By this time I was pretty quick at disassembling the thing
and cleaning the surfaces.

I decided to use rubber gasket material that was nearly
1/8 inch thick.  That allowed for plenty of compression
and there would be no thin areas or missed areas.
To mark the pattern for cutting, I covered the sheet
with masking tape, laid it on top of the base plate,
and pounded around the joint surface with a 5 lb hammer.
The resulting embossed pattern was good enough
to serve as a cutting guide.

While not factory perfect, the result was definitely good
enough: no gaps and the holes aligned.  I was optimistic.

Imagine my disappointment when I found it was leaking 
AGAIN right where it did the first time.  Okay,
time to try tightening the base mounting screws more,
even though I had made sure they were tight before.
This time I disconnected the hoses, flipped
 the head over and tightened the screw in question a bit
 beyond what I thought was prudent.  I went to the max
 even though I was concerned about stripping the slot or
breaking the screw.  It seemed to have stopped the leak
at the base.  HOWEVER...

Now there was a new leak at the intake elbow.  It was difficult
to get a wrench on the nut without disassembling the
head, but I managed to turn it just enough to stop the leak.

But wait...there's MORE!  Also a new leak at the output
elbow.  The engineering geniuses that designed this
put the connection bolt so close to the body that you
can't get a wrench or socket around it.  Fortunately I had a
 set of claw wrenches that could be mounted on the end
of a socket wrench extension, so I was able to barely
get to it and torque it down just enough to work.

I found I had just enough extra output hose length to cut 
off the first inch, hoping it would cure the leak I had 
previously patched with emergency tape.  Good idea;
it just didn't work.  So it was back to the emergency
tape trick, which did work once again.

After pumping through quite a bit of
water and allowing it to sit over night
with no signs of a leak, I remounted
the head and touched up the paint.

So far, so good.  Not counting chickens yet,
though.


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